The Journey – Burning Man 2011 – PDX to BRC

Throwing together a little account of the trip to BRC. Tune in later for the story of the return trip!

It was Friday evening, mid afternoon, and my wife and I had spent the past two days packing and finishing up the last minute projects. Fresh off of the high of NorthWest Mog Fest in Sheridan, OR and the associated shakedown run for The Ghost, we were itching to get in the drivers seat and put some miles between us and PDX. The drive to Black Rock City, NV for the annual Burning Man festival usually knocks out at about 10-11 hours in a ‘normal’ automobile. In a ~20,000lb vehicle that can’t push much more than 65MPH without death shake in the steering wheel, we were expecting to burn a whole day.

Departed that evening and make it about 100 feet out of the driveway. Power loss. Serious power loss. Got out, lightly adjusted the governor gap, and continued motoring. (In retrospect, I should have suspected the fuel tank restriction I have been fighting!). We pushed through some light I-205 and I-5 traffic and headed South to Newberg, OR. We needed to drop off the chickens and grab the last items from the house (my bike, some LMR equipment, etc.) I took the opportunity (while we waited for the temperature to lower outdoors) to adjust the brakes and give a final pre-journey inspection. I needed to grease the cam points on the rear brakes to prevent sticking on takeoff (ongoing issue). After freaking out that the adjustment created a bigger issue , which it actually hadn’t, I gave us the green light on the chassis and we departed.

We screamed down the freeway at a cool 63MPH, engine temps good, overdrive operating as it should, and Marley meowing in her box. We were headed to Corvallis, OR to drop off the cat before heading south. About 10 miles before the Corvallis exit, we lost the ability to go into overdrive. Engine temp was hovering around 180F so we kept motoring on.

Once we reached Corvallis, we ate some dinner (thanks to Barbra) and I started checking out the transmission issue. I read quickly though the manual and troubleshooting section and found that overfull/low can cause overheating of the transmission. I inferred that overheating of the transmission could cause the control pressure to drop (out of the hydraulic governor) and thus drop OD out of the range of the engine RPM. Using their method, I checked the level and found that it was HIGH. The easiest way to lower the volume and keep it clean, I figured, was to remove a pressure line (only 45psi) and put it into a milk jug to catch a quart or two of fluid. So I found a suitable line, disconnected it, and put it into a jug. I started the engine and milliseconds later was douched with hydraulic fluid head to belt line, including the street/tree/bus/curb/grass around me. Fortunately I had kept my hand on the shutdown switch even while starting so I shut the bus off within 2 seconds of the fluid bath (thank GOD for the electric shutdown…the old version required at least 30-40PSI air to shut down!)

After a few hours of cleaning up, and deciding that what was all over the place equated to about 1.5 quarts of ATF, I took a shower, bathed my clothes in liquid dish soap/hot water mix, and loaded up. We had called ahead and determined that the Fred Meyers (of which we had a 10 cent to gallon fuel credit) stopped fueling a 1/2hr earlier. Since we had just acquired about 30 gallons of fuel in Aurora, we decided to motor on and see what was available out by the freeway. Heading out 34 towards I-5, the overdrive engaged and we tore south since fuel prices were >$0.15 higher than other establishments I’d seen closed. I motored until about 2:30AM when I decided to pull it over and catch some rest. By this time, we were a little under an hour down highway 58 headed towards Kalamath Falls, OR. I picked a wide turn-out and crashed out with Emily, who was already asleep in the back.

After a very poor couple hours of sleep, I decided to hit the road again while there was still some chill air at the low altitudes. I motored on, stopping only twice for issues (one the fuel tank screen plugging, the other the overdrive popping out (and thus discovering a small coolant leak in the investigation). Power loss due to fuel restriction is VERY irritating mostly because the bus slowly drops speed (usually when you need the fuel the most) and in some cases, comes to a halt and stalls. The fuel tank screen clearing process was simple, mostly because we couldn’t drain the tank and fix it properly. The on-board air system of the bus had a nice 80-120PSI outlet on the auxiliary air tank that I had a hose and air nozzle to do tire fills, cleaning, or fix this exact problem. I removed the pipe plug just tank side of the fuel inlet check valve and blew all the crap towards the tank and off the screen. Buttoned everything back up and kept on zipping along.

At about 7:45AM, a short distance out of K-Falls (near the lake) I was surprised with a loud POW and the engine racing at much higher RPM. After doing a mirror check, fluid spill check, and gauge scan, I found the next turnout and had a look-see at what happened. It appeared that something had broken in the overdrive system and kicked us out of overdrive, at speed, under load. This equated to a VERY abrupt sudden shift while 500+lbs of iron slinging around at 1550RPM raced to over 2300RPM trying to catch up. Thus…the bang. While I was doing my checks, I found that quite recently the lower coolant hose on the transmission cooler decided to start leaking again where I had previously sealed it up with some Three-Bond and duct tape (classy…I know). With no hose stash, and being a long ways away from a parts/etc. store, I decided to make the same fix again and add some abrasion resistant material to the pipe so it wouldn’t happen again on this trip. Surprisingly, it held the remainder of the trip.

We rolled into K-Falls and hit the NAPA auto parts parking lot. I dissasembled the overdrive valve body and found that the Splitter Clutch Exhaust Valve Spring had broken in two, possibly related to the sudden shift. This spring was in-tact when I checked it in Corvallis, OR, so I rigged up some spacers and whatnot to attempt to regain normal spring length. (This never did function again even after 5 more adjustments stretching and spacing the spring to try and find the magic spot). I also purchased some hose to repair the transmission coolant hose if it decided to fail again. I wanted to also check the rear differential fluid so I walked next door to Autozone and bought a pint of 85w90 gear oil and borrowed a breaker-bar (1/2″ drive) to remove the pipe plug. Turns out the differential didn’t need additional fluid, so we motored on to the Fred Meyers fuel station to get fuel. 67 Gallons later, we pulled out paying about $3.83/gal for fuel (not bad!).

We departed the city and headed out across Eastern Oregon, Northern California, and Finally Northern Nevada. Our only stop as the Eagles Nest Resort (for some transmission tinkering and water fill-up). We departed there after some dinner and cooler air set in for the climb up the final passes before descending into Cedarville and onto the Black Rock Desert. We hit the 12-mile entrance about 7:30-8PM and rolled into camp about 10:00PM.

Overall the trip could have gone FAR worse, but loosing OD on the way down put a crunch in the engine economy. Fortunately it failed at the most ideal time, right when we started climbing hills and would have not wanted overdrive anyway. The Cedarville pass heading down wasn’t terrible as we  had clear roads and climbed most of it in 2nd gear (locked up torque converter) between 35-45MPH. Once we hit the last little bump at the top, it kicked us down to unlocked converter ’1st gear’ and the climb was 18-22MPH. Temperature of the engine/transmission stayed cool enough that we just broke the pass at the 210F mark, and quickly cooled down as we rolled down the other side. The Jaccobs Brakes were a required piece of hardware for those passes and the result was little to no service braking needed for the entire grade. This is an outstanding feat considering many vehicles have overheated and/or lost their brakes going down these hills, only to end up in ditches or off the road. The noise of the jaccobs brakes was difficult to notice from the drivers area, and a medium rumble from the bedroom. We never had to use any emergency braking (either hand lever brake or spring brakes) and air pressure was solid for all climbs and descents.

For the PDX to BRC route, any air-brake equipped coach needs auxiliary brakes of some sort (magnetic, Jaccobs, exhaust, or some type of engine retarding. The pass out of Alturas into Cedarville and also the pass coming down into the desert just north of Gerlach, NV would be tricky. I cannot imagine the long decent at <20MPH burning air pressure constantly on/off the brakes. A suitably strong running diesel with a manually controllable downshift would also be suitable (dynamic braking). Check your slack adjusters, time your compressor to make sure it’s up to snuff, and get out your stop watch to do the decent brake timing. Google it.

A picture of the parking spot, for your pleasure.

A picture of the roadside repairs (attempting to re-gain overdrive somewhere near Eagleville)

The Ghost Update 8/11/2011

Lot’s going on the world of Ghost work!

On the ‘completed’ list, we have the following:
4-valve head installed
Jake Brakes installed (still need to run wire for switch)
Rebuilt Injectors Installed
Coolant Changed
Overdrive Transmission Acquired
Maxi-Brakes Acquired
Bedroom Bed Finished
Bedroom Flooring Installed
Bedroom Door Underway/Built
Kitchen Sink/Faucet Acquired
Kitchen Framed Out
Refrigerator Controller Acquired (for good price!)
Found Power Loss Issue (collapsing govenor to rack control tube)
Water Tank Installed
AC Units Installed and Operational
Acquired Water Pump/Surge Tank/Filters/Drinking Filter
Bedroom Curtains Made!

On the “currently working on” list, we have the following:
Valve Cover Gasket (had to find a different valve cover!)
Govenor Housing Rebuild
Control Tube Replacement (for 4-valve head)
Water Pump Drive Replacement (discovered an immenant failure!)
Rebuild Front Brake Acutators
Building Black Water Tank & Installing
Pouring bathroom floor (sloped for showers)
Frame out Bathroom wall/sink
Install Water Heater
Install Kitchen Sink
Install Stove
Install Refridgerator
Plumb Water System
Install Maxi Brakes and connect to the Switch
Run Jake Brake wiring

On the “potential list” we have:
Install the Overdrive Transmission

This is, of course, in preparation for The Ghost’s virgin Playa Trip down to Black Rock City, NV.

We’ll see how it goes 🙂

The Ghost Update 6/7/2011

Well it has been awhile since we did an update, so here goes.

Currently there is a sizable list of very large projects being worked on for The Ghost. Starting with the most recent, two full power Coleman Mach I Air Conditioner units were mounted to the roof. One mounted just forward of the kitchen area, and one just aft of the bathroom/clothing storage area divider. These units are both mounted offset to the drivers side so that their most extreme points are just inside the outside dimension of the chassis. This works to my favor in the way that I won’t have my head getting knocked on the AC unit ductwork/controls (as with most RV’s) as well as being able to run the ductwork behind the stock wiring/air cavities in the roof of the bus. Units weigh in at about 80lbs a piece and are very low hour usage. Filters for dust and debris will need to be affixed to both the exterior air intakes as well as the interior air intakes to prevent condenser/evaporator contamination. 1500W heating units may eventually be mounted as well inside this AC units.

Another big task on the list is getting the updated (1960’s) 4-valve head inspected, rebuilt, and ready to swap out in place of the original 2-valve. The main factor in wanting to make this upgrade is the increased availability of Jake Brake assembles for 4-valve heads. The 2-valve head Jake Brakes are quickly approaching impossible to locate, so this upgrade should yield acquiring a set of Jake Brakes for ~$400. The potential head for rebuild came from Dan off a motor that dropped a couple valves and locked up. We’ll see if it is rebuildable. A note on this, a pretty serious inspection of the existing engine required determining if it was of the ‘low’ or ‘high’ block design. The low block being much older, uses a different head-gasket (which is almost impossible to find) and some strange ports on the engine where the newer ‘high block’ does not. Fortunately, it appears The Ghost currently houses a 6-71 Detroit High Block (2-valve). Yay!

With the head, the 6 fuel injectors also need rebuilt, so those are currently in the shop getting rebuilt and balanced within 10%. A few had stuck racks, which can indicate water intrusion, but injectors are easy to come by (relatively) so the replacement rebuilt units should be ready soon.

The water tank was recently ordered (expensive!) however at 125 gallons, it was worth buying a quality marine grade tank that will last for a very long time. Material of choice in this case is a drinking water safe poly (3/8″ wall thickness!). This will be located on the starboard side aft of the rear axle under the sleeping area but inside the passenger compartment to help prevent freezing and road damage. That should arrive soon via freight (also expensive for some reason).

Bedroom/bathroom walls are up, and the door is cut and ready to weld together (1″ aluminum box). Need to insulate and sheet the remaining areas and start working on the bathroom floor. The black water (toilet) tank will likely be made out of stainless steal or some other coated metal to optimize the tank size under the coach (odd shaped compartment, but lots of available volume). I will likely have this sheet plasma cut out, and then weld it together and seal the seams to prevent issues with porosity later down the road.

All the wheels/tires have been upgraded to 22.5″ currently BUDD style rims with new lug nuts/bolts where needed. The ride is very nice with radial ply tires versus the old bias ply design.

A fuel sender was also recently affixed to the fuel tank (mounting/hole already existing!) so that fuel level can be determined via gauge instead of dip tube or guess work. Currently this is a universal sender (Stewart Werner type) and the gauge is a positive ground 12V unit I scored off of ebay. Works good. A 14″x14″ hole was cut in the floor directly above the fuel tank to allow access to the sender for future repairs/adjustments. There is also a breather located nearby that may eventually need service and not having to drop the tank would make this access port well worth while.

The new FanTastic RV vents are working wonderfully and without any water leaks to the exterior. These powered 12V auto open/close w/ rain detector vents make camping a breeze. Now just to have them somehow detect dust and close when the dust storms come 🙂

Once the water tank arrives, I will start fabricating the bed/desk/clothing storage areas. Sound and heat insulation will be affixed wherever possible.

Soon to be also upgraded will be the rear brake actuator so that they can operate with an Emergency Brake mode (so I can stop the bus if I am out of air). The foot valve, a D1, was recently rebuilt on my living room table and I posted a how-to since that is a VERY old rare foot valve to still be on the road. Working flawlessly now and air loss from the main tanks now is far less of an issue when the coach is parked. The windscreen wiper controls are the next biggest source of leak.

Well that is all for now. Many other small fixes here and there have been done…feel free to stop by and check it out if you desire.